Sorry for your loss of a good friend.
What in particular did you see as being different or disqualifying as to not being within the profile of a typical PLM accident? I think it checked all of the boxes except maybe the pilot being thoroughly familiar with the potential hazard.[/quote]
Part of it is that Ron knew to check, especially coming out of maintenance. The main thing is the airplane pitched up and came back down, instead of turning left and rolling over.
I also have one bit of insight that I can not share publicly, I'll just say that I am not the only one that suspects it was something else.[/quote]
Here is the final report and some excerpts
It did turn left and eventually rolled over in a similar manner as other PLM suspected crashes. The potential health issue was covered in the report. I don’t think it was a factor.
I think that it supports a strong likelihood of a PLM occurrence. Like I have said before I would not put much merit on post crash trim tab and tab control positions. The cables get tugged differentially when an aircraft essentially cartwheels and breaks apart. I don’t buy the tab positions as evidence that he didn’t use a checklist.
https://asn.flightsafety.org/asndb/319129Narrative:
A Beechcraft 200 Super King Air, was destroyed following a takeoff accident at Chicago/Rockford International Airport (KRFD), Chicago/Rockford, Illinois.
The purpose of the flight was to relocatr the airplane to the pilot's home base near Wayne, Illinois. The airplane was at a repair station at Rockford Airport for maintenance work. Shortly after liftoff from runway 19, the airplane started turning left, and the airplane developed a large left bank angle as it was turning. The airplane departed the runway to the left and impacted the ground. During the impact sequence, an explosion occurred, and there was a postimpact fire.
An NTSB airplane performance study showed that during the takeoff, a nose-left sideslip, a left side force, and a left roll occurred, consistent with the loss or reduction in thrust of the left engine.
The sideslip was reduced, likely due to inputting rudder to balance the side force, and the airplane briefly rolled right possibly due to an overcorrection in rudder. The airplane pitched up and was able to begin climbing again; however, it continued to lose speed. The sideslip then reversed, and the airplane rolled left again before impacting the ground. The study indicated
that before rotating and lifting off, the airplane accelerated to a groundspeed of 98 knots (kts) and an airspeed of 105 kts, which was about 19 kts above the published minimum control speed for the airplane. Therefore, the airplane had achieved sufficient airspeed for the pilot to maintain control despite a loss or reduction in left engine thrust provided he made the
appropriate control inputs. The sideslip force calculations indicated that there was a partially successful attempt to maneuver the airplane back to level flight when the airplane rolled back right, but it was not maintained.
Teardown examinations of the engines and propellers found no evidence of preimpact failure.
Analysis
The pilot departed on a positioning flight in the twin-engine airplane. Videos recorded by
multiple airport-based cameras showed the airplane take off from runway 19. Shortly after
liftoff, the airplane started turning left, and the airplane developed a large left bank angle as it
was turning. The airplane departed the runway to the left and impacted the ground. During the
impact sequence, an explosion occurred, and there was a postimpact fire.
An airplane performance study showed that during the takeoff, a nose-left sideslip, a left side
force, and a left roll occurred, consistent with the loss or reduction in thrust of the left engine.
The sideslip was reduced, likely due to inputting rudder to balance the side force, and the
airplane briefly rolled right possibly due to an overcorrection in rudder. The airplane pitched up
and was able to begin climbing again; however, it continued to lose speed. The sideslip then
reversed, and the airplane rolled left again before impacting the ground. The study indicated
that before rotating and lifting off, the airplane accelerated to a groundspeed of 98 knots (kts)
and an airspeed of 105 kts, which was about 19 kts above the published minimum control
speed for the airplane. Therefore, the airplane had achieved sufficient airspeed for the pilot to
maintain control despite a loss or reduction in left engine thrust provided he made the
appropriate control inputs. The sideslip force calculations indicated that there was a partially
successful attempt to maneuver the airplane back to level flight when the airplane rolled back
right, but it was not maintained. The right rudder input would need to be held until the thrust
asymmetry was corrected.
Teardown examinations of the engines and propellers found no evidence of preimpact failure.
Both engines exhibited evidence of operation at impact. Damage to the propeller blades and
hubs indicated that neither propeller was feathered at impact. The predominant left propeller
Page 1 of 11blade bending and twisting was aft and toward low pitch. The predominant right propeller
blade bending and twisting was forward in the thrust direction and toward high pitch. Analysis
of the propeller internal witness marks and the blade damage found that the right engine was
producing more power than the left engine at initial impact. Based on the available evidence, it
could not be determined why the left propeller was not feathered at impact, even though the
autofeather system was armed.
The rudder trim knob was found 4 units to the left; the aileron trim knob was found 6 units to
the right; and the rudder boost switch was found in the OFF position. The before engine
starting checklist in the pilot’s operating handbook for the airplane specified that the rudder
and aileron trim be set and that the rudder boost switch be on. Therefore, the postaccident
positions of the rudder trim knob, aileron trim knob, and rudder boost switch likely indicate the
pilot did not follow the before engine starting checklist. With the rudder boost switch not being
on, it could not be determined based on the available evidence, what role that system may
have had with the pilot attempting to maintain control of the airplane during the asymmetric
thrust sequence.
Although the pilot’s previous history of significant coronary artery disease and the scar in his
left ventricle placed him at increased risk of an acute cardiac event, whether such an event
occurred at the time of the accident could not be determined from the available information.
Absent evidence of an engine malfunction, the investigation considered whether the left
engine’s thrust reduction was the result of a malfunction in the throttle control system or an
uncommanded throttle movement due to an insufficient friction setting of the airplane’s power
lever friction locks. However, heavy fire and impact damage to the throttle control system
components, including the power quadrant and cockpit control lever friction components,
precluded determining the position of the throttle levers at the time of the loss of thrust or the
friction setting during the accident flight. Thus, the reason for the reduction in left engine
thrust could not be determined.
Probable Cause and Findings
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The pilot’s failure to maintain airplane control following a reduction of thrust in the left engine
during takeoff. The reason for the reduction in thrust could not be determined based on the
available evidence.